Where to from here...?

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Trailstar

Well-Known Member
Posts
554
Range Rover Classic
3.5 on Lpg
Put new exhaust system on, then first start the vehicle overheated, drained coolant, flushed radiator, new thermostat, new temperature sender...and it still over heated...
So I decided to pull the water pump off....
20190126_202818.jpg

But the rotors appear fine!?
20190126_202829.jpg

Now I have had this vehicle for a good 3 months, and it's never overheated, almost run a bit too cool.....until just recently

So any advice would be appreciated!!!
 
It's got 1 hot dog silencer, and we cut some ugly restrictive repair bits out of the section b4 the Y, and then installed a 2.5" rear section that we had pre bent up.........so definitely not restrictive!!!

That's the bit that gets me is that it decides to do it now......I could accept that the water pump is inefficient if it had always run hot but it's always run pretty cool.....
 
Range Rover Classic
3.5 on Lpg
Put new exhaust system on, then first start the vehicle overheated, drained coolant, flushed radiator, new thermostat, new temperature sender...and it still over heated...
So I decided to pull the water pump off....

But the rotors appear fine!?

Now I have had this vehicle for a good 3 months, and it's never overheated, almost run a bit too cool.....until just recently

So any advice would be appreciated!!!

Well the damage to the pump housing shouldn’t have happened, obviously that damage can only be done by the pump. It looks as if there wasn’t a gasket and just red sealer was used, so that would have placed the impeller closer to the housing, or of course an iffy pump bearing allowing the impeller to wobble but that’s something u would hear.

So if the impeller is slipping on the shaft ie become detached and isn’t turning, therefore no coolant circulation within the engine, the engine will overheat. If not slipping look else where.
 
Water pump looks like it’s been cavitatiing, did you drain coolant to fit exhaust, and not bled properly, or it’s pumping compression gas straight in there from head gasket failure
 
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