N
Nige
Guest
Got Monty back from the garage today, runs sweet as a nut, but the cutting
out every 6 or 7 seconds is still there. It's passed it's test. I have a
thought about this. The chap mentioned it was blowing crankcase fumes into
the dizzy. He thinks is possibly a worn piston on number 7 (low comp) The
more I think about it, he said he took the cap off & there was pressure
there. This missing could be caused by the whole dizzy getting pressurized &
the cap lifting to release the fumes under pressure. Anyone think this is
possible, if so, can I drill a vent hole in the cap or assembly?
The cap & rotor he took off where melted & really fumed up.
I'm not really bothered by the miss, I can drive around it, but the cap &
rotor arm are gonna get fried again.
The crank vents are all clean too.
Any thoughts?
Ta
Nige
out every 6 or 7 seconds is still there. It's passed it's test. I have a
thought about this. The chap mentioned it was blowing crankcase fumes into
the dizzy. He thinks is possibly a worn piston on number 7 (low comp) The
more I think about it, he said he took the cap off & there was pressure
there. This missing could be caused by the whole dizzy getting pressurized &
the cap lifting to release the fumes under pressure. Anyone think this is
possible, if so, can I drill a vent hole in the cap or assembly?
The cap & rotor he took off where melted & really fumed up.
I'm not really bothered by the miss, I can drive around it, but the cap &
rotor arm are gonna get fried again.
The crank vents are all clean too.
Any thoughts?
Ta
Nige