hello everyone .
3 half years ago I rebuilt my 12j engine .
This was a full nut bolt gasket everything done job .
Crank polished
Block skimmed & honed “020”
Head skimmed& valves polished
Injector pump rebuilt
Cam & followers had minimal wear .
I had a break down other day & got recovered, this is the problem .
As you can see the gasket between 1 & 2 has completely failed , it was from turner engineering so a very good gasket in my opinion.
Why would this have happened so quickly ?
The manuals say to re use the old head bolts, they don’t state any mileage for a re torque “probably due to cast iron head “ ??
I did re check the torque after couple hundred miles btw & all was ok .
I can’t seem to find a similar thread on here .
3 half years ago I rebuilt my 12j engine .
This was a full nut bolt gasket everything done job .
Crank polished
Block skimmed & honed “020”
Head skimmed& valves polished
Injector pump rebuilt
Cam & followers had minimal wear .
I had a break down other day & got recovered, this is the problem .
As you can see the gasket between 1 & 2 has completely failed , it was from turner engineering so a very good gasket in my opinion.
Why would this have happened so quickly ?
The manuals say to re use the old head bolts, they don’t state any mileage for a re torque “probably due to cast iron head “ ??
I did re check the torque after couple hundred miles btw & all was ok .
I can’t seem to find a similar thread on here .