I've just been going with this on mine today.
One little wrinkle made the mixture adjustment screw do absolutely nothing - and that was that, on removing the screw, the groove down it was COMPLETELY blocked with old varnishey muddy gunk.
MOT fail on mine was very low CO (~0.15%) and slightly too high HC (~1400ppm), which wasn't a surprise, since the lack of any kind of idle meant that I had to leave the choke on a whiff - but it ran beautifully.
The idle screw (throttle stop) wouldn't screw in enough to idle, so I've moved the locking collar to the back. Idle as low as it'll go without dying, and mix set 1.5 turns out, then out until it sounds nicer.
It's now idling and pulling reasonably smoothly, but has gained a bit of a "fluff" accelerating hard in third. It doesn't seem to start quite as easily as it did, either.
We'll see what it comes up to on the MOT machine, and what we can get it to.