Thanks mate!! Shall look into ittheir is a piece on removal in landrover monthly dec 2017
. apparently they say takes around six hours so I have never tried .hope this might help.
should read ... "can reattach the egr to the ecu" ...Busy removing egr cooler for replacement with new unit. Egr & cooler come off as a unit.
After an oil change, I noticed I had over filled after running the engine. Corrected oil level whereafter I experienced white smoke from exhaust, exhaust bubbling in expansion tank, aircon heater runs cold, hissing noise from exhaust and coolant disappearing with no external sign of a leak. Car starts and runs fine, did not run the engine for long so no signs of overheating. Other causes could be head gasket failure or manifold failure.
Purchased a new egr cooler, but have decided to fit the new unit blanking off the exhaust port and egr port and connecting the coolant hoses to bypass the cooler. Thus the new egr cooler with new gasket and cleaned egr will be present should I need to use the egr in future.
There is a freelander2_Manual in pdf format online that describes the procedure. The space behind the engine is very confined, accessing bolts
(hex & allen key type) is by touch in some cases, a torch and mirror helps. Disconnect the wiring harness and remove brackets to create more
work room. A paper clip helped to release the egr harness plug and a flat band plier helped with the cooler inlet hose clamp.
With the egr cooler off I will check the unit to be sure that this is the cause of coolant entering the exhaust. I'll then cut off the inlet and outlet ports and weld these together to create an adapter to link the coolant hose.
Unfortunately it does take awhile to remove the egr, if you just intend blanking the ports and connecting the coolant hoses to delete the egr unit then there is no need to fit a replacement egr - there will be more space behind the engine in future.
Having a replacement egr attached means that I cant reattach the egr to the ecu circuit ... have not had any issues yet with the engine check light.
I have attached a collage of the EGR repair. Note the features of the respective EGR coolers differ, specifically the original has 32 gas ports and a large chamber clearly intended to maximize exhaust gas transfer to the engine. The new (Jul 2017) cooler drops the large chamber but retains the
32 gas ports increasing the amount of coolant that can circulate between the ports and likely reducing the volume of exhaust gases that are drawn into the EGR valve chamber. A bypass tube was fabricated from the salvaged port tubes of the original cooler, to be used to reroute coolant from the egr cooler thus it is only exhaust gas that passes through the egr cooler to reach the egr valve. The efficiency of a cooler can reduce by 25% to attain a stable state. The amount of heat transferred from gas @ ~375° to a 32 vane cooler @ ~103°C may be negligible and the increased efficiency of coolant passed to the radiator is believed by some to compensate for this loss in egr cooling. The bypass can also be used temporarily if there is uncertainty regarding the functioning of the egr valve or if a head gasket failure is still a concern.
The collage shows evidence of coolant crystals present in the egr valve ports. Moreover, the accumulated soot with coolant coating the head can
be mistaken for a head gasket failure.
A tapped hole in the exhaust aft of the manifold is an easy solution to draining the exhaust of fluids, a bolt or screw is then seated to plug the hole. Two alu 3mm blanking plates are available for blanking of the egr circuit at the exhaust manifold and egr vacuum hose should the effect
be warranted.
Following the repair and recharging with coolant (bring engine up to temperature to open thermostat, drain and recharge. Run HOT aircon to purge heater core) all symptoms disappeared:- exhaust gas bubbles in expansion tank, white smoke from exhaust, poor idle unblanked and rapid loss of coolant (with no visible leaks). Noticed that cold start is easier, the engine reaches temp sooner, the engine sounds smooth and am anticipating improved mpg.